Carriage & Wagon Report June 2006
article by: Richard Johnson
I see, looking back through these reports that I first began
mentioning work on the FK (Corridor First) 13329, over a year ago.
It really has taken that long to restore, and we chose to do it
because at first glance it appeared to be in 'good' condition.
It is now complete bar the shouting, and was moved outside on
10th June. As I write, there are a few bits of trim to be screwed
back, floors to be given a final clean and one or two minor
plumbing dribbles to be attended to. Then, it's into traffic for
the first time. Buy a First Class ticket and judge for yourselves
what you think.
Our RBr (Restaurant Buffer Car) 1675 performed sterling service
throughout the nine days of our Gala. I am told that the bacon
rolls went down well. This was a baptism of fire for it, and no
mistake. Nine days continuous running; sometimes from 9.00am until
9.00pm. Inevitably a couple of problems manifested themselves as
the week wore on. Firstly, a valve on the pressurised water system
stubbornly stuck open and meant that pressure could not be raised
properly, leading to a lack of water for drinking, cooking and
washing up. Secondly the thermocouple on the boiler failed towards
the end of the week. We have decided to take the coach out of use
again for a short period to rectify these things. We cannot do it
whilst it is in service.
As was said before, it is inevitable that in bringing back into
use equipment that is 45 years old, and has not worked for the last
10 years, there are bound to be teething problems until it all beds
down. We will get there.
Currently in our shed on a temporary basis, and receiving
attention is Mk 1 TSO (Tourist Second Open) 4763. I have attached a
picture, showing work on the roof going ahead. The work is being
done at the toilet end, where a number of pipes and vents protrude,
and some holes have been discovered. This is the second of the two
TSO's we rescued from the Paignton & Dartmouth Railway a couple
of years ago. 4772 has already been restored and is in the
Chocolate & Cream set.
There is plenty to do on 4763, so all the effort being put in
now will shorten its ultimate restoration. This is actually quite
useful, as it gives us the measure of the job, and means we can
keep that in mind and make plans, whilst working on the Maroon
set. One job we have not tackled before has become apparent.
The section of the steel vacuum pipe which protrudes from one end
of the coach by the buffers is badly corroded and has some big
holes in it. After much head scratching, we have decided that to
get to it to get it out and replace with new, we are going to have
to strip out one of the toilets, and take up the toilet floor!
The GWR Tool Van W4 is making good progress. This vehicle has
four large glass roof lights, to give plenty of light to those
working internally. A broken one has been replaced, and serious
repairs are underway to the pair of windows on the sliding doors at
each side. The only real major job left on the body itself is to
replace the roof canvas. That should be interesting with the four
roof lights above mentioned!
A project just being started is the restoration of an LMS 6
wheel passenger Brake Van 32990, known as a 'Stove R'. This belongs
to the 8F Group of which Loco Department Head Mike Hoskins is a
member. Apparently, they have a complete set of parts, and all new
replacement cladding. We dragged it out of the siding where it had
been hiding for several years, and it will go under cover just as
soon as the GWR Tool van is finished. I have also attached a
picture of this. It can be seen that it is in need of complete
strip down and refurbishment.
These vehicles are quite rare in preservation. They were
apparently built for use on goods trains, such as milk trains or
some parcels trains which had no train heating. Thus a stove was
installed to keep the Guard warm. The plan is to get it refurbished
and operational into full 1938 LMS livery, exactly as it was when
first built 68 years ago. That should look good.
After 20 years of running without a bogie problem on our
coaches, we have now had two in two weeks. Firstly, the SO (Second
Open) 4787 had to be withdrawn during the Gala, after a strong
smell was noticed from one of the axleboxes. Examination showed
that it was running hot, so the coach was detached to be checked.
When we opened up the axle box, we found that the bearing had
actually sheared, and the part bearing on the journal had twisted,
causing heavy wear into the bronze. I have attached a photo of what
we found.
Although not absolutely clear, the picture shows the bearing
standing on end and at the top, it is showing bronze where it
should be white metal. On the left is the part that had sheared
off. The rectangular plate it is resting on is the slipper plate
that sits above it in the axle box. Happily, the journal
itself does not appear to be damaged.
A week later, we had a similar report from a Guard about the
Carmine & Cream RMB (Buffet). Examination showed shards of
white metal on the axlebox pad, so that coach has had to be
withdrawn to be checked out.
It is ironic that we should have experienced these problems, as
for the last couple of years we have had a serious continuing
programme to overhaul the axleboxes on all our service coaches, to
make sure that they are in tip top condition. There has been a
beneficial change to the oil used, and a pad renewal programme is
underway.
Next time, I will be able to deal with this a bit further.
Hopefully, I will be able to report that all is well.